This is a chronicle of my custom-built multi-system passive radiator,
system water blocks, and accompanying water distribution system. I
continually update this page with the latest developments and
additions, so check back often!
 Passive Cooling Tower
My current apartment windows are not well suited for attachment of
ducts, and I am quite a bit more ambitious now. I aim to achieve
good performance with a passive air cooling, and thus absolute silence.
Over the past two years, I have built a central radiator, a number of heatsinks for components in and out of the computers, and the accompanying monitoring system to evaluate performance. With the radiator passively cooled, I achieve water temperatures 9-10C above ambient, and component temperatures well below that of any air-cooled heatsink. Including all piping, the system holds about 6 gallons. See the live Machine Status section for current performance statistics.
For the sake of simplicity, I have separated most photos into the sub-sections at left. Please refer to them for complete construction details.
Design & Operation
Pump
I currently have an Iwaki MD15RLT pump. This is an external pump rated at a max of 5.0GPM, or 11.1ft head. It draws 0.28 amps. Full flow curves are available on the Iwaki site. As I have no desire to pump any more water than necessary to cool my machines, this pump is more than adequate. Sold as one of the quietest aquarium pumps available, it is nearly inaudible and produces minimal vibration. Be sure to note that the Japanese model Iwaki pumps (MD) have a different motor than the American models (WMD). While identical in pumping characteristics, the American models are less energy efficient, producing more heat and noise.
Any noise produced by the Iwaki MD15RLT is easily dampened by the thin 1/4" plywood panels on my pump cabinet. All vibration is easily dampened by a sheet of 1/2" Elastic Foam Rubber from McMaster Carr. In a silent room, the pump cabinet produces no audible noise beyond 2-3 feet.
For a little more than a year, I did use a Little Giant PCL-020 pump. This is a submersible pump with ratings similar to the Iwaki. With nearly identical pumping characteristics to the Iwaki(both in specification and practice), this pump drew around 0.7 amps. Additionally, significant amounts of vibration were produced, even when dampened with rubber. Increases in this vibration as it aged finally prompted me to purchase the Iwaki, which should easily last 5 years before repair with easily available parts.
I
achieve about 1.5GPM flow with the entire system connected. Given the
temperature differentials I see across the radiator, I believe the
cooling efficiency to be quite high. I see about a 1C temperature
differential between inlet and outlet temperatures of the radiator.
According to my UPS, I am drawing anywhere between 300 and 350W
depending upon load. See the Temperature Sensor section for measurement methods. Real-time flow rates and temperatures are on the Machine Status page.
Radiator
The purpose of the radiator design was to achieve the greatest
cooling with absolute silence, with an eye toward aesthetics. The
current final product has evolved a bit, but the basic design has
remained throughout. It is based upon a 6" single-walled tin
pipe, commonly used for kitchen hood vents. This was epoxied very
firmly to a tera-cotta pot base, which was cut with much effort to
allow pipes to pass through the center. The 1/2" flexible copper
refrigeration pipes (type L) were then spiraled singly around this frame.
The original plan called for one tube, but when the flow seemed too
little, I added a second in parallel. I could still add more, and
in fact left the plumbing open to expansion, but wrapping the pipe is
extremely difficult. I wanted the coil to be tight but kinks were
very easily formed with this large of tubing. It finally worked
to roll the tubing onto the center pipe, maintaining a good amount of
tension on the spool. This was definitely a two-person job.
If I were to recommend any change, I'd suggest a more flexible variety
of tubing, or find a large spring to prevent kinks, at the risk of a looser wrap. See the Radiator Photos for pictures of the final product. Unfortunately, there are few photos of actual construction. (No spare hands were available.)
Reservoir (New)
To eliminate any concern of leaks and plastic incompatibility, I am now using a molded polyethylene boat water reservoir from West Marine. The smallest tank they offer (Model 486639) is 3 gallons and provides two 1-1/2" and one 1/2" NPTF connections. I used PVC fittings to reduce from such large fittings and to create a manifold for the return and output. Thermometers were included in both pipes.
Before switching to the external Iwaki pump, power was run through the 1/2" connection using a rubber grommet. After cutting an appropriate hole, a boat deck plate (Model 103622) was used to provide access to the pump. In hindsight, I underestimated the size required for my pump and was forced to disassemble the pump impeller to get it inside. Internally, the pump wass connected with clear flexible tubing which fits tightly inside the final 3/4" reducer. In tests, PVC glue was stronger than my ability to remove it, so this tube was glued as well. To eliminate vibration, the pump had zip-ties run through a few pieces 1/4" plastic tubing and secured around the pump. As much of the produced sound had been from pump vibration against the reservoir, this was quite effective. For further construction details, take a look at Reservoir Photos.
Hard Drive Cooling
 Mounted Hard Drive Cooler
When I purchased my Koolance case for my desktop, I was impressed
with the hard drive cooler. Using a thermal encapsulate for conduction
to the circuit boards and spindle-motors on each side, the aluminum
water-block is sandwiched between 2 disks. Disk temperatures never have
gone measurably above that of the water. However, it's far from
economical. Last I checked, the cost was upwards of $70 for a 2-disk kit.
This cost put me a bit above what I thought was reasonable for
cooling my 4-disk SCSI raid-5 array. Half-height(1.62") disks, they
require substantial mounting hardware and dissipate about 11W each. As
usual, I forged ahead with a custom solution. After empirical testing to be sure
that the drives would in fact conduct a significant amount of heat to
a copper plate secured to their sides(using hot water), I constructed a copper drive cage/water cooler for them. 1/4" copper tubing, often used for
ice makers, was bent and soldered to two copper plates, one for each
side. I obtained the 1/8" copper plate for about $30 from McMaster Carr. See the Hard Drive Photos for construction details.
Power Supply (New 2/8/2005)
 Power Supply (without case)
I have recently found time to modify one of my Fortron 400W ATX power supplies to be water cooled. Similar to the hard drive coolers, I have soldered 3/8" copper tubing to 1/8" plate, which is secured to the major heat producing components. The particular power supply I modified has two large aluminum heatsinks, providing a convenient flat surface to attach to. By drilling and tapping four holes in these heatsinks, the copper plate was securely bolted, with a moderate amount of heatsink compound to improve thermal conductivity. See the Power Supply Photos for construction details.
Of some concern are components in the supply which are not directly attached to the main heatsinks and would ordinarily depend upon some amount of airflow for proper cooling. With no fan at all, improper cooling of these components would result in elevated ambient temperatures within the power supply case. I have monitored this with my 1-wire sensors. Without the absolute loss of air exchange in the rackmount case, ambient temperatures have increased throughout, typically remaining from 90-110F, with the highest inside the power supply. Of course, the temperature of all water-cooled components has remained static. Informal spot checks indicate that no components are in excess of normal temperatures. Additionally, ambient temperatures respond within minutes to increase or reduction in water flow, suggesting good heat transfer from those components responsible for the elevated ambient temperature. (When I get a chance, I'll post more formal test results.)
Measuring Flow (Updated 1/5/2006)
 Dwyer Visi-Float Flowmeter
I now have two flowmeters; one for total flow, and another for the rackmount machine. The total flow meter is a George Fisher Signet 515-X0 Rotor-X Paddlewheel Flow Sensor. This sensor outputs 6Hz per ft/s. The 3/4" PVC tee I am using has a K-Factor of 257.72 in US gallons. That is, the sensor outputs 257.72 pulses per gallon. To allow logging, I use a Dallas/Maxim DS2423 to count the pulses. Dividing the difference between timesteps by the K-Factor gives me a very accurate measurement of total flow rate. Note that the 515 is only usable down to 1ft/s, or 6Hz. With the 3/4" tee, this results in a minimum accurate flow of about 1.4GPM, or 83.8GPH--just below my approximately 90GPH flow. While I used a 3/4" tee to avoid restricting flow in my PVC lines, a 1/2" tee would probably be a better choice. It has a K-Factor of 480.19. Another choice is the Signet 2536, which can measure to 0.3 ft/s.
The rackmount machine has a Dwyer Visi-Float VFB 5-60GPM flowmeter. It has 1/8" NPTM connections on back, to which I attached the incoming water lines from the hard drives and the outgoing line to the power supply and motherboard coolers. See the Rackmount Photos for details. eBay often has new flowmeters at very reasonable prices. Find out as much about liquid compatablity as possible before purchasing.
Unresolved Issues
Electrolysis
From the beginning, I knew I had the potential to create a battery with
dissovled ions in the water. I had no idea that I could achieve
upwards of 0.25V between a copper pipe in the reservoir and the
radiator. Given that both are copper, I'm still puzzled about why
there is any potential whatsoever. I don't believe the pump is
leaking current, since the voltages persist even when the reservoir is
tied to ground. In addition, higher concentrations of antifreeze
seemed to increase the observed potentials. Since the system is
grounded at all possible points(both computers, tower, and reservoir),
and since I've seen no real corrosion, I am merely puzzled, not
concerned. I'd of course like to be able to explain it. See the Coolant Compatibility and Electrolysis section for more details.
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